Gaps in Hazard Analysis and Emergency Response Contribute to the Fatal KMCO Texas Explosion:

Gaps in Hazard Analysis and Emergency Response Contribute to the Fatal KMCO Texas Explosion:

(CSB) report summary:

On April 2, 2019, KMCO was producing sulfurized isobutylene as a lubrication additive. The explosion and fire occurred after isobutylene leaked from a fracture in a segment of piping and formed a flammable vapor cloud, which ignited.  

One employee was fatally injured, and two others were seriously injured.  At least 28 other workers were also injured.  

CSB Chairperson Steve Owens said, “The tragic death and injuries caused by this terrible event should never have happened.  KMCO did not properly train its employees and did not give them adequate protective safety equipment.  KMCO also failed to heed industry guidance about the need to install remote isolation equipment so that its employees could have safely stopped this serious hazardous leak.”    

The CSB’s final report determined that the isobutylene release occurred when a piece of equipment called a y-strainer ruptured due to brittle overload fracture. Specifically, the cast iron y-strainer was installed within an area of the piping system that, unlike other portions of KMCO’s isobutylene piping, was not equipped with a pressure-relief device or otherwise protected from potential high-pressure conditions. Therefore, when those conditions developed, most likely due to liquid thermal expansion, the y-strainer was subject to high internal pressure and ruptured releasing isobutylene which formed a vapor cloud. This flammable cloud most likely ignited from contact with electrical equipment within a poorly sealed, nearby building.  

The CSB’s report identified three key safety issues that contributed to the severity of the incident. They are:   

  1. Emergency Response. KMCO’s procedures and training did not properly limit the role of its operators during the emergency response. KMCO’s plant culture relied on unit operators taking quick actions to stop a release before the site’s emergency response team assembled. While those urgent communications and quick actions did help move many operators away from the danger, the workers performing the quick actions were at risk. KMCO could have reduced the severity of the April 2, 2019, event by establishing clear policies and training its work force to not put themselves in danger at all to urgently stop a chemical release.
  2. Remote Isolation. When the y-strainer ruptured, KMCO’s workers lacked the safety equipment they needed to stop the isobutylene release from a safe location, such as from within the blast-resistant control room.
  3. Hazard Evaluation. Hazard evaluation is one of the most important elements of a process safety management program. KMCO’s hazard evaluations consistently overlooked or misunderstood that its y-strainer was made from cast iron, a brittle material that existing industry standards and good practice guidance documents either prohibit or warn against using in hazardous applications, such as KMCO’s isobutylene system. 

Following the April 2, 2019, incident, KMCO filed for bankruptcy, and the company is no longer in business. 

www.mycontrolroom.com

Alex Taimuri, P.Eng., MBA

Passionate to constantly elevate myself, our team, our clients and our world as a whole, one project at a time.

11mo

Thanks for sharing this Stephen. Sad to see this, as proper training and updated procedures could have potentially prevented this. Richard Jones Mehdy Touil Gabrielle Hebert

To view or add a comment, sign in

Insights from the community

Others also viewed

Explore topics